News:

We have implemented a Photo Gallery for hosting images right here on SAACFORUM. Check the How-To in News from HQ

Main Menu
Menu

Show posts

This section allows you to view all posts made by this member. Note that you can only see posts made in areas you currently have access to.

Show posts Menu

Topics - Brad Griffith

#1
Ad up now on Hemmings as of 10/2. Never advertised before other than here on SAAC. Selling my 1965 K Code Fastback GT. Solid, San Jose car, always in California (until last year in TX), so NO rust. I have photographed the undercarriage, and it is painted black, but lots of orange oxide underneath. Appears all original. Perfect pinch welds on both sides. Very nice example. Not a survivor, etc, but a solid, sorted, terrific car to drive. Everything I can think of works. Factory color is Silver Mist, which is a great color in my opinion. Black interior, which is a color change from original red. Previous owners added a correct 4 point roll bar and 1966 Shelby Quarter windows. Job was well done. Has a T5 5 speed, Currie rear axles with larger rear drums as in the original GT350's. 9" rear end of course, 3.50 gears, which mate perfectly with the 5 speed. I always liked 3.89's with a top loader, but the first gear ratio on a T5 is lower, so this is perfect. VERY fresh K code engine, with Edelbrock aluminum heads, 715 Le Mans Holley, Comp cams Hydraulic camshaft and high quality Cobra reproduction aluminum intake (Not made in China, but a Blue Thunder version). I wish it had my favorite Comp Cams 271S camshaft, as those will pull to 7k rpms if the rest is done properly. This engine and cam combination is very strong down low, and pulls hard to 6K RPM's. Erson aluminum rockers. Cobra oil pan, correct dual point distributor with Petronix guts and a yellow top coil. 1" Shelby drop has been done, and it has the Standard GT-350 quick ratio pitman and idler, front disks. Correct style Monte Carlo bar, Ford export brace, and reinforcing plate for export brace is welded on the cowl. Front crossmember is very heavy duty, and has an integrated jack pad. The Undercarriage is unbelievably tidy: spin tech mufflers, new driveshaft for T5, and sub frame connectors from Global West Suspension. Painted black, underneath, but you can see red oxide poking through in many places. Great pinch welds on both sides. Trunk mounted battery. 1965 Shelby style tachometer and oil pressure pod on dash. Runs very strong. 14" 1966 style Shelby 10 spokes with fresh tires. New Maier springs in rear, and 600 pound springs in front. The undercarriage is unbelievably clean and tidy. Clutch is fresh. More pics soon, and if you have genuine interest, please call. $75k. I will answer all questions as honestly as possible, tell you what I know, and what I do not. Absolutely 100% complete and full disclosure. Also, what I would personally do with the car if I were to retain it (Hint, not much! :)) Price firm. Thanks for your interest. Brad@ 214.507.9441 Please call, do not text. Or you can DM me, or email me at griffbl@me.com
#2
Wanted to Buy / WTB: Pinion Snubber Bracket for 65' Hipo
December 19, 2021, 10:25:16 AM
I would like to find a nice Pinion Snubber Bracket for Ford 9" rear end in my 65' K code. Later variation of bracket which was used 68-73 is fine also, as it was used as a service replacement. Would like a nice one with limited pitting. Thanks for your help. Email me at Griffbl@me.com. Thanks!  Brad
#3
Wanted to Buy / WTB: 1965 or 1966 K Code Fastback
June 17, 2020, 08:40:00 AM
Must be a four speed, preferably Wimbledon White or Black.  Some Other colors considered. Standard interior hopefully, and non GT package would be perfect. If it needs mechanical work that is ok, but body must be solid. Many thanks! 214.507.9441
#4
Here is the kind of great information for which I love this forum so very much, so thanks in advance for your help.

When I was the caretaker of 5s287, my Holley 715 was SPOT on. It was that way when I bought the car from Brett.  That car was a tad stronger than stock, and had what I thought was a slightly more aggressive solid cam than a stock hipo camshaft.  My 66 GT350 was supercharged, so it had a mechanical secondary Holley. My 67 Gt350 had a perfectly set up Le Mans carb also.  I have good luck with them so far.

Today, my black 65' K code is the project at hand. The engine has a .030 over bore, with correct TRW pistons, aluminum heads (painted black) with 53cc combustion chambers. I had the combustion chambers cut to that size so as to be about 10.5 to 1 as to compression ratio. Intake ports are matched to an original 66' Shelby dual plane intake manifold. Competition Cams Nostalgia Plus series 271s solid cam, (more aggressive than a Hipo cam, and with modern tight lash of .012 hot) and roller tipped rockers. They fit under the standard hipo valve covers after I modified one of the baffles . Standard Hipo distributor with Petronix components, probably 14 degrees initial timing and another 20 mechanical advance for 34-36 total. No pinging. Jim Cowle's beautiful coated Try Y Headers, T style Cobra oil pan and an Arvinode exhaust.  I would like for them to exit on the side like a 65 GT350, but being a factory GT I needed to exit the rear valance. Car is light.  Again, aluminum heads, edelbrock painted black aluminum water pump, standard GT non-pony interior, (no console etc.) 66' package tray, no spare inside car, aluminum cragar reproductions, aluminum water pump, radio delete, I pulled the heater, fan, heater core, etc.  Detroit locker with 3.89's.  Car runs very strong.  Wheel hop initially was terrible, so I went with the Maier Racing springs that cured my traction problems.  These springs are probably about equal in weight to standard Hipo springs plus Shelby traction bars (or a bit less) as they are 4 1/2 leaf springs vs. 4 leaf factory springs. Problem solved. ( as an aside, the original Shelby traction bars on my 5s287 really DID work! That car just kind of squatted and jumped up.  I had 235 60's in back and that helped also). This car makes lots of power.  More than did 5s287 did under my care.  I am guessing about 360 horses at the flywheel. Maybe a tad more, but I think that is close.

Back to my carb problem.....My reproduction 3259 Carb was purchased new, recently, by me at Branda. Confirmed primary idle transfer slots exposed a small "square". Engine making 12"(varied a bit from 11-13") or so of vacuum at idle. Idle set at about 750-800 RPMs... Had stock 68 & 78 jetting. Seemed to have a lean bog from a stop and every time gears were shifted when full throttle applied. With the 68 primaries, I had the idle mixture screws turned out 1 1/2  to 1 3/4 turns or so. I bumped up the primary jets to 70's from 68's. That seemed to help reduce the bog some. Now, best vacuum is about 1/2 turn out on the idle mixture screws, as the 70's are allowing more fuel. I bought a Holley Vacuum quick change spring kit, and an Accelerator Pump Cam kit. Currently has the stock white cam in position one. Next we changed the stock 25 Squirter nozzle to a 28, and changed to a white (lightest) vacuum secondary spring from the stock yellow spring.  Other than the slight hesitation at throttle application, car ran great and pulled hard. VERY.

We thought we might have a vacuum leak given the variations as to idle vacuum. We checked, none found. We pulled the carb to check a couple of things and to use a slightly thicker carb baseplate gasket between it and the intake manifold which we preferred to the thin paper one we were using.  We tried 69's as primary jets, as with the 70's installed, and we could bottom the mixture screw on the driver's side and it would still run. Car did not run better, and now we could bottom both idle mixture screws and the car would continue to run. Car had backfired once as we were working on it (it never has in other situations) and I suspected we blew the power valve, which is a failure condition that would allow the engine to continue to run with the idle mixture screws bottomed out. Power valve was the stock 8.5.  We tried a 6.5, as depending on which set of Holley instructions you follow, either can be called for.  Of course a 6.5 delays the secondary fuel delivery, and the car clearly ran worse. We went back to the stock 8.5 valve, and back to the 70 jets.  Adjusted mixture screws again to about 1/2 turn out. Peak vacuum at idle now approaches 15", which is very good given this cam with just under .5" of lift. Car runs great, but still has a slight hesitation on throttle application, but less than before. I have been checking to see that our accelerator pump lever is adjusted properly also.
Our plan is to now maybe A) try a different color accelerator pump cam?, and or maybe B) a slightly bigger squirter from the 28 we are now using. Going from a 25 to a 28 was a definite improvement before. Any other ideas? It seemed to run better when we increased the pump squirter before, so we thought we might try another bump up maybe from a 28 to a 30?
Also, The engine will now idle with the idle screws bottomed. It is my understanding that this is caused by either 1) an idle that is so high as to over ride the idle circuit or 2) a blown power valve or 3) improperly set float levels or 4) improperly adjusted butterflies vs.the transfer slots.  Front float level is set at 1/2" from the factory and that is my understanding to be correct. So I don't know what is causing this condition.  We did not pull the rear float bowl and check the rear float adjustment.  The secondaries do seem to be closed entirely at idle, and appear to be as they should be.  No visible signs of fuel dribbling in.

So that is question 2, what could be causing the mixture screws to bottom and the engine still idle?

Many thanks!

Brad